I have a Craftsman DYT 4000 with a B&S 24 hp Intek. It has been running really rough last cutting, then this time it started skipping enough to notice, before it was more of a surge. I replaced the air filter this spring, and cleaned the carb and air filter/pre cleaner last week. It started up a lot better, and ran for about 1 hr before doing the same thing again. I also noticed with the surging it only done it when it got hot. I also changed the furl filter last week as well, lots of what looked like rust around the outside of plastic bowl (loose) mower has a plastic gas tank.
The mower has been kept well, has 100 hours on it at present. I use Stabil for the gas. I purchased it on sale new, the next season time for grass cutting and at 8 hours the left intake vale stuck. I removed the head, pushrod was bent and valve had a lot of glued on carbon gunk. I cleaned it off, fixed the bent pushrod, polished it, set valve clearance and no problems until now. I consider this one of the worst purchases I have ever made, the motor in my opinion is junk to have this many problems already !! If anyone has had, and fixed this problem I would appreciate some pointers. I also changed the plugs last season trying to fix the surging problem, I'm thinking it has got to be in the carb since it did help for a little while, but how to fix the problem for a short time.
The mower has been kept well, has 100 hours on it at present. I use Stabil for the gas. I purchased it on sale new, the next season time for grass cutting and at 8 hours the left intake vale stuck. I removed the head, pushrod was bent and valve had a lot of glued on carbon gunk. I cleaned it off, fixed the bent pushrod, polished it, set valve clearance and no problems until now. I consider this one of the worst purchases I have ever made, the motor in my opinion is junk to have this many problems already !! If anyone has had, and fixed this problem I would appreciate some pointers. I also changed the plugs last season trying to fix the surging problem, I'm thinking it has got to be in the carb since it did help for a little while, but how to fix the problem for a short time.